Improving ESP Performance in Low Productivity Gassy Wells: Case Study

Author:

A. Salah Ahmed Salah1,A. Sabaa Ahmed Sabaa1,A. S. Abd Elhaleem Ahmed Samir Abd Elhaleem1,Shehab A. Shehab Ali1,S. Ritondale Sergio Ritondale1,A. Sorou Amin Sorour2,A. Nady Ayman Nady2

Affiliation:

1. Agiba Petroleum Company

2. Hultic Limited Borets

Abstract

Abstract The electrical submersible pump (ESP), has become the most efficient and reliable artificial-lift method worldwide. However, in wells with high gas volume, they are highly affected by gas bubbles flowing through each component, affecting: the motor temperature, lifting efficiency, the integrity of the motor and cable. Thus, High gas interference might cause multiple intermittent shutdowns due to Gas Lock and eventually shorten the run life of the ESP. ESP at Well #A was first installed and directly had a problem with High Gas Interference resulting in a pre-mature ESP failure and costly well intervention to restore well-deferred production. A detailed discussion with a technology provider and reference case studies come up with an integrated solution to have the proper gas handling system in addition to adjusting VSD logic to operate on PID current mode. The present study shows a successful ESP optimization through VSD settings in combination with a comprehensive gas handling system that allowed management of low productivity high GOR ESP applications. This gas handling system for ESP was complemented by installing [PMM motor, tandem gas separators with vortex technology, compression mixed-flow stages in a wide range centrifugal pump, advanced gas handler (AGH), and Monel armor leaded power cable]. The system was able to manage GOR>2,000 SCF/STB with WC of <10%, Productivity index of 0.2 BPD/psi, and 75% of free gas flowing into the pump intake. This paper contains all the descriptions of each component in the ESP gas handling system. The system was able to increase well production by reducing gas-locking production shutdowns, stabilizing motor current fluctuations, increasing ESP lifetime, and increasing reservoir life by increasing drawdown and allowing effective pump operation at lower intake pressure. The same directions were successfully applied in another two wells with low productivity gassy behavior; Well #B and Well #C. And, by monitoring ESP performance for a longer period, the pump showed a stable operation, by successfully mitigating the high gas interference trips. Thus, the implementation of this integrated solution in wells with high GOR has been demonstrated to be an effective solution. Also, it provides opportunities to expand the use of ESP in gassy wells, previously thought to be unsuitable.

Publisher

IPTC

Cited by 1 articles. 订阅此论文施引文献 订阅此论文施引文献,注册后可以免费订阅5篇论文的施引文献,订阅后可以查看论文全部施引文献

1. Superior Short circuit & Overcurrent Protection of Devices like Alternator, Transformer etc.;Journal of Image Processing and Intelligent Remote Sensing;2022-03-14

同舟云学术

1.学者识别学者识别

2.学术分析学术分析

3.人才评估人才评估

"同舟云学术"是以全球学者为主线,采集、加工和组织学术论文而形成的新型学术文献查询和分析系统,可以对全球学者进行文献检索和人才价值评估。用户可以通过关注某些学科领域的顶尖人物而持续追踪该领域的学科进展和研究前沿。经过近期的数据扩容,当前同舟云学术共收录了国内外主流学术期刊6万余种,收集的期刊论文及会议论文总量共计约1.5亿篇,并以每天添加12000余篇中外论文的速度递增。我们也可以为用户提供个性化、定制化的学者数据。欢迎来电咨询!咨询电话:010-8811{复制后删除}0370

www.globalauthorid.com

TOP

Copyright © 2019-2024 北京同舟云网络信息技术有限公司
京公网安备11010802033243号  京ICP备18003416号-3