Author:
Nhut Huynh Tan,Hung Nguyen Tri Quang,Sac Tran Cong,Bang Nguyen Huynh Khanh,Quang Tri Tran,Trung Hiep Nguyen,Minh Ky Nguyen
Abstract
This study evaluates the efficiency of domestic wastewater treatment via Sponge-Based Moving Bed Biofilm Reactor (S-MBBR). The laboratory-based treatment plan uses polyurethane sponge with a specific surface area was 260 m<sup>2</sup>/m<sup>3</sup> as a carrier. The treatment plan operated under four different organic load rate: OLR1 = 0.4 kg BOD/m<sup>3</sup>.day; OLR2 = 0.6 kg BOD/m<sup>3</sup>.day; OLR3 = 0.8 kg BOD/m<sup>3</sup>.day; and OLR4 = 1.0 kg BOD/m<sup>3</sup>.day. During 80 d of the experiment, the highest treatment efficiency was at the organic load rate of 0.4 kg BOD/m<sup>3</sup>.day, with COD, SS, TN and TP were found to be 85.0 ± 12.9%, 85.7 ± 5.3%, 68.9 ± 1.7%, and 40.3 ± 0.2%, respectively. In which, the influent SS concentration were from 117.3 to 126.0 mg/L, the effluent concentration were in ranged 18.0 to 34.22 mg/L, respectively. The values of influent and effluent COD were 298.8 ± 12.88 and 44.8 ± 3.78 mg/L in turn. The OLR1 influent TN, TP concentrations were respectively 47.9 ± 2.11 and 3.6 ± 0.15 mg/L; the effluent TN, TP concentration were 14.9 ± 0.18 and 2.2 ± 0.06 mg/L, respectively. The study suggests that the effluent is within the allowable limits of National technical regulation on domestic wastewater (Column B1), indicating the applicability of S-MBBR for the domestic wastewater treatment plant.
Funder
Nong Lam University
International Environmental Research Institute
Gwangju Institute of Science and Technology
Publisher
Korean Society of Environmental Engineering
Subject
Environmental Engineering
Cited by
22 articles.
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