Cause Analysis of Buttress Premium Thread Connection Pullout for a Well

Author:

Pan Zhi Yong1,Song Sheng Yin1,Liu Wen Hong1,Wang Jian Jun1,Wang Xin Hu1

Affiliation:

1. Tubular Goods Research Institute of China National Petroleum Corporation

Abstract

The buttress thread connection was used in deep well or ultra-deep well widely because of its high joint efficiency. Pullout failure scarcely happen on buttress premium thread connection with great joint strength and good sealing property. Direct evidences about connection dropout couldn’t get in most cases by reason of casing string had fallen into well or casing string had been concreted in formation by cement. Now the difficulty of analysis on pullout is higher and higher. A buttress premium thread casing joint had pulled out at mill end of coupling in a straight well and dropout casing string couldn’t get out of the well. Research on this pullout case was carried out combining relative theories with tests. Macroscopic analysis and dimension measurement were done for dropout coupling. The material’s physical and chemical properties were checked. Thread inspection and full-scale tests were done for two casing simples that are same lot with pullout. Metallograph analysis was carried out on load flank and guide flank in box thread of pullout coupling and same lot new coupling. The results showed that dropout failure was ascribe to inadequate make-up torque at mill end of pullout coupling and complex downhole condition and improper handling in the oil field. On the other hand joint’s strength decline on the effect of unsuitable heat treatment to coupling and greatly uneven black crested pin thread around circumference. The pertinence measures were laid down at the end of this passage.

Publisher

Trans Tech Publications, Ltd.

Subject

General Engineering

Reference10 articles.

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3. Shi Jiaoqi, Han Xinli, Zhao Kefeng, et al. Adaptability of buttress thread casing for ultra-deep holes [J]. China Petroleum Machinery, 1998, 26(11): 24-28.

4. Ji Bingyin, Lu Shuanlu, Zhang Hong. Calculation on tension strength of non API size casing with buttress thread connection [J]. Oil Field Equipment, 2011, 40(2): 58-62.

5. Gao Lianxin, Shi Jiaoqi, Jin Ye. Influence of make-up torque on the connection strength of round thread casing [J]. Natural Gas Industry, 2005, 25(2): 87-89.

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