Water Wall Tubes’ High Temperature Corrosion Root Cause Investigation: A 300 MW Level Boiler Case

Author:

Xiong Xiaohe1,Chen Falin1,Li Liangyu1,Tan Houzhang1

Affiliation:

1. MOE Key Laboratory of Thermo-Fluid Science and Engineering, Xi’an Jiaotong University, Xi’an 710049, China

Abstract

High temperature corrosion poses a great threat to boiler water wall safe operation. To investigate the corrosion root cause, a 300 MW level boiler water wall high temperature H2S corrosion case was reported. The typical hydrogen sulfide H2S corrosion feature was large amounts of sulfur which could be found in the cut down sample tube corrosion layer, with a thickness of 482 μm. In addition, huge amounts of lead (Pb) could be found in the corrosion layer, which resulted from the lead sulfide (PbS) deposition when the high temperature flue gas condensed at the water wall tubes. Meanwhile, the sulfur in the corrosion layer was closely related to the H2S concentration in the water wall ambience. The related ambience test showed that the H2S could achieve up to 1000 ppm when the boiler was in operation, far larger than the suggested reference value of 100 ppm. Hence, the overlarge H2S concentration was a vital factor for the tube corrosion. To further investigate the reason why the H2S was kept in such high concentration in the boiler long term operation, and the reasons for the over-high sulfur content in the coal and the over-large diameter of the imaginary circle of primary air (DICPA), two factors were obtained. The peak sulfur content reached 2.5% and the suggested sulfur content was below 1%. The DICPA was so large (1580 mm) that the pulverized coal easily scoured the water wall tubes, which would boost the thinning process of the tubes. To relieve the high temperature corrosion, improve the coal qualities, decrease the DICPA, adjust the operation diameter and adopt a coating technology four measures were suggested.

Funder

National Natural Science Foundation of China

Publisher

MDPI AG

Subject

Energy (miscellaneous),Energy Engineering and Power Technology,Renewable Energy, Sustainability and the Environment,Electrical and Electronic Engineering,Control and Optimization,Engineering (miscellaneous),Building and Construction

Reference25 articles.

1. Policy and management of carbon peaking and carbon neutrality: A literature review;Wei;Engineering,2022

2. Research on influence of steam extraction parameters and operation load on operational flexibility of coal-fired power plant;Wei;Appl. Therm. Eng.,2021

3. (2022, December 30). Action Plan for Energy Conservation and Emission Reduction Upgrading and Transformation of Coal Fired Plants 2014–2020. National Development and Reform Commission, Ministry of Ecological Environment, National Energy Administration, China. EB/OL, Available online: http://www.gov.cn/gongbao/content/2015/content_2818468.htm.

4. Study on high temperature corrosion mechanism of water wall tubes of 350 MW supercritical unit;Sun;Eng. Fail. Anal.,2021

5. Experimental research of mitigation strategy for high-temperature corrosion of waterwall fireside in a 630MWe tangentially fired utility boiler based on combustion adjustments;Xu;Fuel Process. Technol.,2019

Cited by 3 articles. 订阅此论文施引文献 订阅此论文施引文献,注册后可以免费订阅5篇论文的施引文献,订阅后可以查看论文全部施引文献

同舟云学术

1.学者识别学者识别

2.学术分析学术分析

3.人才评估人才评估

"同舟云学术"是以全球学者为主线,采集、加工和组织学术论文而形成的新型学术文献查询和分析系统,可以对全球学者进行文献检索和人才价值评估。用户可以通过关注某些学科领域的顶尖人物而持续追踪该领域的学科进展和研究前沿。经过近期的数据扩容,当前同舟云学术共收录了国内外主流学术期刊6万余种,收集的期刊论文及会议论文总量共计约1.5亿篇,并以每天添加12000余篇中外论文的速度递增。我们也可以为用户提供个性化、定制化的学者数据。欢迎来电咨询!咨询电话:010-8811{复制后删除}0370

www.globalauthorid.com

TOP

Copyright © 2019-2024 北京同舟云网络信息技术有限公司
京公网安备11010802033243号  京ICP备18003416号-3