Performance degradation analysis of a medium pressure superheater due to tube deactivation

Author:

Haqim Ahmad Syafiq,WAN MOHAMED WAN AHMAD NAJMI,Tijjani Al Hassan Salami

Abstract

Steam is essential in petrochemical industries for the transportation of thermal energy and usage in some reforming process. Superheaters are heat exchangers that convert saturated steam to dry steam by utilizing waste heat from the flue gas stream. Medium pressure steam superheaters are prone to tube deterioration due to service at elevated temperatures and erosion from the presence of liquid phase in the steam, leading to tube plugging after tube failure. This reduces the overall surface heating area of the superheater. Relations between the tube plugging practice and the energy dynamics of the superheaters are important for engineers to identify the responses of the superheater for operation planning, and this issue has not been extensively explored academically. This article analyses the deterioration of superheater performance due to reduction of surface heating area based on operational data of a petrochemical steam generation line. The objective is to find relations between the effect of tube plugging on the states of both steam and flue gas streams, as well as its impact on the overall energy exchange. The operating conditions of a superheater at two separate service years, before (year 2014) and after (year 2017) tube plugging, were compared through the first law energy analysis. The average steam inlet temperatures were between 248 °C and 250 °C, at flow rates between 70 and 90 ton/hour. The analysis indicated that 0.3 to 0.8 % increase in inlet energy is required for every plugged tube to compensate for the reduction of heating surface. At 3 % reduction of heating surface area, the heat exchanger effectiveness decreases by an average of 11 % that also leads to a lower steam temperature output by approximately 6% from the design operating temperature. These results would assist steam engineers to analyse changes to the energy economics of the whole plant and decide the feasibility of replacing existing superheaters with new ones. Also, another significant finding to be considered by steam engineers is that the current practice of increasing the steam flow rate does not offset the loss of energy effectiveness due to tube plugging.

Publisher

Universiti Malaysia Pahang Publishing

Subject

Industrial and Manufacturing Engineering,Mechanical Engineering,Mechanics of Materials,Energy Engineering and Power Technology,Fuel Technology,Computational Mechanics

同舟云学术

1.学者识别学者识别

2.学术分析学术分析

3.人才评估人才评估

"同舟云学术"是以全球学者为主线,采集、加工和组织学术论文而形成的新型学术文献查询和分析系统,可以对全球学者进行文献检索和人才价值评估。用户可以通过关注某些学科领域的顶尖人物而持续追踪该领域的学科进展和研究前沿。经过近期的数据扩容,当前同舟云学术共收录了国内外主流学术期刊6万余种,收集的期刊论文及会议论文总量共计约1.5亿篇,并以每天添加12000余篇中外论文的速度递增。我们也可以为用户提供个性化、定制化的学者数据。欢迎来电咨询!咨询电话:010-8811{复制后删除}0370

www.globalauthorid.com

TOP

Copyright © 2019-2024 北京同舟云网络信息技术有限公司
京公网安备11010802033243号  京ICP备18003416号-3