The Role of Auto Driller, Rig Control Systems and Driller Procedures in Reduction of BHA Failures

Author:

Barajas Pablo E.1,Pastusek Paul1,Lacey Aaron1,Sharp Matt1,Whitlow Zack2,Glenn Landon2,Melton Micah2,Menand Stephane2,Holder Bradley2,Kendrick Stephen2,Witt-Doerring Ysabel3

Affiliation:

1. ExxonMobil Upstream

2. Helmerich and Payne

3. Halliburton

Abstract

Abstract Reducing bottom hole assembly (BHA) failures has been the focus of this operator in US land intermediate and lateral sections to reduce cost per foot. BHA failures can be mitigated with better auto driller processes, improved rig control system technology and drilling mechanics based procedures. The operator, rig contractor and BHA service providers engaged in an intensive continuous improvement process for 18 months to help two rigs in Oklahoma reduce BHA's per well. The goal was to determine how to best tune the auto driller and standardize set point practices. By investigating this for each stand drilled, the plan was to improve bit run footage and reduce BHA tool failures per hole section. The rig contractor deployed a system upgrade and adjusted driller procedures to help identify auto driller dysfunction quicker. In-bit sensors that measured drilling parameters, vibration and strain were run to validate suspected downhole dysfunction and premature bit failure. The operator's procedure to quickly evaluate and mitigate auto driller dysfunction was trialed to distinguish rig control system induced dysfunction from downhole drilling mechanics dysfunction. For the Oklahoma rigs, auto driller stability was evaluated and improved in ∼50 BHA runs in the 12-1/4″ intermediate hole sections and in ∼100 BHA runs in the 8-3/4″ lateral BHA runs. Motor failures in the 12-1/4″ intermediate section and in the 8-3/4″ lateral sections were reduced, as were premature bit failures. Also, it was found that tool joint hang-up in the rotating head were exciting the rig control system into dysfunction and causing a significant reduction in downhole weight on bit (WOB), differential pressure (DP) and rate of penetration (ROP). These hang-up events were occurring 3 times per stand, and although ROP would recover after the tool joint exited the rotating head, damaging vibrations at the bit continued long after the ROP recovered. The operator's tool joint compensation procedure was implemented in subsequent runs and lateral bit vibration and dull condition improved substantially. The learnings from the auto driller continuous improvement process were cascaded to two additional rigs in another basin in East Texas. Reducing depth of cut (DOC) variance through ROP set point management in interbedded formations reduced required bit runs in the second basin as well. The rig contractor deployed an upgraded auto driller system to minimize parameter variance and extend the life motors in high temperature laterals reducing the risk of catastrophic failure. And the rig contractor and operator continue to develop and trial auto driller dysfunction alarms to alert to possible BHA dysfunction. New tools, processes and scorecards are being developed to aid in the identification of dysfunction in rotary and slide drilling.

Publisher

SPE

同舟云学术

1.学者识别学者识别

2.学术分析学术分析

3.人才评估人才评估

"同舟云学术"是以全球学者为主线,采集、加工和组织学术论文而形成的新型学术文献查询和分析系统,可以对全球学者进行文献检索和人才价值评估。用户可以通过关注某些学科领域的顶尖人物而持续追踪该领域的学科进展和研究前沿。经过近期的数据扩容,当前同舟云学术共收录了国内外主流学术期刊6万余种,收集的期刊论文及会议论文总量共计约1.5亿篇,并以每天添加12000余篇中外论文的速度递增。我们也可以为用户提供个性化、定制化的学者数据。欢迎来电咨询!咨询电话:010-8811{复制后删除}0370

www.globalauthorid.com

TOP

Copyright © 2019-2024 北京同舟云网络信息技术有限公司
京公网安备11010802033243号  京ICP备18003416号-3