Simulation of Horizontal Wells to Mitigate Miscible Solvent Gravity Override in the Virginia Hills Margin

Author:

Chugh S.1,Baker R.1,Cooper L.2,Spence S.3

Affiliation:

1. Epic Consulting Services

2. Shell Canada Ltd.

3. Woodside Energy Limited

Abstract

Abstract Significant incremental recovery can be obtained when vertical sweep is improved in the mature Phase I Miscible Flood area of the Virginia Hills Field. This study advances our knowledge of the gravity override processes operating in this complex carbonate reservoir. Furthermore it shows that horizontal injection wells improve sweep efficiency thereby alleviating the impact of solvent gravity override. As a result of this simulation, a successful horizontal injection well was drilled, with an actual 18 E3m3 incremental oil recovery to date and a predicted 65 E3m3 total incremental oil. The results of this study suggest redevelopment in mature EOR areas is expected to extend the life of the miscible flood and increase overall recovery. Introduction Miscible recovery in the Virginia Hills Field Hydrocarbon Miscible Flood (HCMF) project is significantly limited by poor vertical sweep of the solvent within individual layers of the reservoir. A vertically continuous interval within the reef margin (30 m thick) was investigated and shown to have a large bypassed tertiaryoil target. This study demonstrated that recovery could be significantly increased through the use of horizontal solvent injection wells. To have confidence in the results of the study it was critical to utilize geological and production history data to address the interwell extent of significant heterogeneities. This required complete integration of geological and engineering staff in all phases of the study. Background Historical The Virginia Hills Beaverhill Lake A Pool was discovered in 1957. The field (Figure 1) produces oil from a Mid-Upper Devonian limestone, stromatoporoid build-up. The field was unitized in 1963 and a waterflood pressure maintenance scheme was implemented. In the late 1980s the patternswere normalized to inverted nine spots and in 1989 a tertiary horizontal hydrocarbon miscible flood project was initiated in the south half of the Pool. The original oil in place (OOIP) for the pool has been calculated at 59.6 E6m3 by the operator. Cumulative oil production to the end of July 1996 was 22.9 E6m3, or 38.4﹪ of the OOIP. Current oil rates of 1,000 m3/d have fallen from peak rates of 4,400 m3/d. Field average water cut is greater than 90%. Within the EOR area, well spacing is 32 ha., approximately 400 m interwell distance. Geological The internal architecture of this limestone reservoir is multilayered and compartmentalized, due to several stages of carbonate accumulation. From the base up these stages are: S1 (equivalent to the regionally extensive Slave Point platform), S2A, S2, S3L, S3U, and S4, (herein called S-units) reaching a total maximum thickness of 150 m. A high energy windward margin exists along the eastern portion of the build-up with superior reservoir quality (an average range of.09 to.12 phi, and 20 to 120 mD permeability). For this study the S3L in the margin area of the build-up was investigated (Figure 1). Solvent Gravity Override Solvent gravity override (Figure 2) occurs when there is sufficient time for injected solvent to segregate prior to its withdrawal due to gravity differences and therefore a smaller miscible oil target is swept.

Publisher

Society of Petroleum Engineers (SPE)

Subject

Energy Engineering and Power Technology,Fuel Technology,General Chemical Engineering

Cited by 6 articles. 订阅此论文施引文献 订阅此论文施引文献,注册后可以免费订阅5篇论文的施引文献,订阅后可以查看论文全部施引文献

同舟云学术

1.学者识别学者识别

2.学术分析学术分析

3.人才评估人才评估

"同舟云学术"是以全球学者为主线,采集、加工和组织学术论文而形成的新型学术文献查询和分析系统,可以对全球学者进行文献检索和人才价值评估。用户可以通过关注某些学科领域的顶尖人物而持续追踪该领域的学科进展和研究前沿。经过近期的数据扩容,当前同舟云学术共收录了国内外主流学术期刊6万余种,收集的期刊论文及会议论文总量共计约1.5亿篇,并以每天添加12000余篇中外论文的速度递增。我们也可以为用户提供个性化、定制化的学者数据。欢迎来电咨询!咨询电话:010-8811{复制后删除}0370

www.globalauthorid.com

TOP

Copyright © 2019-2024 北京同舟云网络信息技术有限公司
京公网安备11010802033243号  京ICP备18003416号-3