Abstract
AbstractWell completion practices in high-temperature, high-pressure carbonates are challenging especially for long lateral horizontal wells intended for fracturing applications. An integrated approach involving intervention and fracturing design and reliable post-fracturing flow measurements is very critical to optimize the well performance.After initial intervention complexities due to wellbore accessibility in a 6,250-ft cemented lateral initially planned with 13 fracturing stages resulting in the loss of many operational days, a revamped engineering workflow was planned for Well-A. As a first step, Coiled Tubing (CT) was used for abrasive jetting perforations, cleanout, and acid squeeze functionalities with a novel bottomhole assembly (BHA). The BHA was equipped with a real-time telemetry to optimize intervention to a single run. Having real-time bottomhole parameters helped in perforating the desired zones accurately and enhanced the injectivity by creating cleaner perforation tunnels.Stages were reduced to five with an optimized perforation design based on rock typing approach, and short clusters were designed to divert the fracture fluids effectively using multimodal particulate diversion. Each fracturing stage was isolated with a mechanical plug. A novel high-frequency pressure monitoring technique that analyzes fluid entry points from water hammers was utilized during the fracturing treatments to analyze on-the-fly diversion efficiency and optimize further treatments.A multiphase flowmeter was utilized to enhance milling and flowback to minimize losses and manage the choke schedule based on actual well performance leading to better fracture cleanup and recovery. The production performance of Well-A was compared with two offset horizontal wells drilled azimuthally parallel, intersecting the same carbonate sublayer. The post-fracturing absolute production enhancement analysis showed 11 to 15% improvement, and productivity index (PI) improvement was 40 to 63% when normalized by stage count. The effective integration of multiple technologies was applied successfully on the candidate well, yielding enhanced operational efficiency with optimized production performance.
Cited by
7 articles.
订阅此论文施引文献
订阅此论文施引文献,注册后可以免费订阅5篇论文的施引文献,订阅后可以查看论文全部施引文献
1. Fiber Assisted Enhanced CO2 Foam Fracturing and Proppant Placement;Day 1 Mon, October 16, 2023;2023-10-09
2. Digital Degradable Chemistry Provides Solutions for Production Enhancement and Intervention in Challenging Wells;Day 2 Wed, September 13, 2023;2023-09-12
3. Comparative Look at Wellbore-Rock Connection Techniques – An Integrated Perspective from Stimulation, Intervention and Laboratory Research;Day 2 Wed, March 22, 2023;2023-03-14
4. Implications of Wellbore-Fracture Separation on Temperature Log Interpretation Studied Through Numerical Modeling and Field Measurements and Observations;Day 2 Tue, March 14, 2023;2023-03-13
5. A Workflow to Assess the Effect of Lateral Landing, Completion, and Fracturing on Production Potential in an Explorational Clastic Environment;Day 2 Mon, February 20, 2023;2023-03-07