Affiliation:
1. Department of Mechanical Engineering, Korea Advanced Institute of Science and Technology, Daejoen 34141, Korea
2. Development Group, Turbocharger Division, Mitsubishi Heavy Industries Engine & Turbocharger, Sagamihara Kanagawa 252-5293, Japan
Abstract
Abstract
The effects of turbocharger rotation inertia on instantaneous turbine efficiency were analyzed in a 2.0 L four-cylinder twin-scroll turbocharged gasoline direct injection (T-GDI) engine. Two turbochargers of different weights were prepared for comparison purposes: base T/C and light T/C. In order to evaluate the instantaneous efficiency of each turbocharger, a combination of engine tests and a 1D simulation was conducted. In the experiments, the instantaneous exhaust gas pressures, upstream and downstream of the turbine, were measured. The instantaneous turbocharger rotation speed was also measured. The instantaneous temperature and mass flow rate of the exhaust gas were taken from the 1D simulation results. Through a combination of measuring and simulating exhaust gas states for the turbines, the instantaneous turbine blade speed ratio (BSR), total-to-static turbine efficiency (ηts), reduced mass flow rate (φ), and reduced turbine speed (Nred) were calculated. The light T/C showed higher fluctuations in the instantaneous turbine rotation speed compared to the base T/C. This greater response from the light T/C is due to experiencing less inertia loss, this leads to higher fluctuations in the instantaneous Nred, BSR, ηts, and φ. As a result, the light T/C shows higher turbine efficiency at certain points after the start of the exhaust gas pulse cycle. This is because the greater response of the light T/C lead the operating conditions of the turbine to more efficient regions in the turbine map.
Funder
Mitsubishi Heavy Industries
Subject
Mechanical Engineering,Energy Engineering and Power Technology,Aerospace Engineering,Fuel Technology,Nuclear Energy and Engineering
Cited by
3 articles.
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