Abstract
Injection coupling is a well-known cause of high-frequency combustion instability in hydrogen/liquid oxygen ([Formula: see text]) rocket engines. This type of instability is commonly explained by the two-way coupling between the dynamics of the combustion chamber and the injection system. Recent experimental studies of the BKD combustor, however, suggest that the LOX injector could be self-excited and driving the acoustic mode of the combustion chamber. To assess the feasibility of this mechanism, here, we study both experimentally and theoretically the acoustic stability of the LOX injector isolated from the combustion chamber. The experimental study was performed in a water facility mimicking the conditions of a single LOX injector. The water injector was then modeled using an acoustic network analysis, where the transfer matrix of the LOX injector inlet orifice was computed numerically using a linear approach. The analysis successfully predicts the experimental peak in unsteady pressure, revealing that the LOX injector can be self-excited. The instability was found to be driven by the whistling of the orifice at the inlet of the injector coupled with the second longitudinal acoustic mode of the LOX post tube.
Funder
ERC Consolidator Grant AFIRMATIVE
Publisher
American Institute of Aeronautics and Astronautics (AIAA)
Cited by
1 articles.
订阅此论文施引文献
订阅此论文施引文献,注册后可以免费订阅5篇论文的施引文献,订阅后可以查看论文全部施引文献