Experimental analysis of acidizing in Weizhou X low permeability reservoir

Author:

Zhang Yi12ORCID,Zhang Bin12,Wei Feng3,Lu Hongjun4,Liu Banghua5,Tang Mingguang3,Zhu PengYu2,Wang Rui12,Yan Jian1

Affiliation:

1. Shaanxi Key Laboratory of Well Stability and Fluid & Rock Mechanics in Oil and Gas Reservoirs Xi'an Shaanxi China

2. School of Petroleum Engineering Xi'an Shiyou University Xi'an Shaanxi China

3. Development Department of Zhanjiang Branch of CNOOC (China) Zhanjiang Guangdong China

4. Oil and Gas Technology Research Institute of Changqing Oilfield Branch of CNPC Xi'an Shaanxi China

5. CNPC Production & Operation Management Department Beijing China

Abstract

AbstractAiming at the problem of increased water injection pressure and poor water injection effect during the water injection operation of Weizhou X offshore low permeability oil reservoir. The cause of clogging was clarified using cast thin section experiments, water quality compatibility experiments and reservoir sensitivity experiments, and corresponding deblocking agents were configured based on the experimental results. The experimental results show that Weizhou X oilfield has strong velocity sensitivity (damage rate 85.35%) and strong salt sensitivity (damage rate 63.02%), and there is a phenomenon of water quality incompatibility. Analysis shows that the excessive velocity of the injected water causes the core particles to fall off and the water quality is incompatible with the calcium carbonate precipitation to cause pore throat blockage as the fluid migrates to the small roar, which is the main reason for the increase in water injection pressure. Based on the analysis results, the acid solution formula was optimized and determined to be: 12% HCl + 0.5% HF + 3% CH3COOH + 0.5% C6H12N4. Indoor test results show that the acid has good clay swelling prevention and reservoir modification effects, and the average reservoir modification rate is 129.21%. The plug‐removing effect is remarkable and can be promoted in similar oil fields.

Funder

Key Research and Development Projects of Shaanxi Province

National Natural Science Foundation of China

Publisher

Wiley

Reference26 articles.

1. Research on the water channeling mechanism and influencing factors of low permeability oil reservoirs—taking X area of Ordos Basin as an example;Su X;Inner Mongolia Petrochem Ind,2020

2. Research on reservoir damage during water injection development of low porosity and low permeability oil reservoirs in Moriqing oilfield, Yitong Basin;Wang Y;J Saf Environ,2016

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